Showing posts with label refrigeration. Show all posts
Showing posts with label refrigeration. Show all posts

Sunday, January 18, 2015

Refrigeration System Ducting

We've always wondered about the efficiency of the Sea Frost condenser and compressor system. It is in the same compartment as the port hot water heater. The engine cooling water loop runs from the bulkhead to the hot water heater, adding its heat to the compartment. To try to gain a little more efficiency out of the existing unit, we took two measures.

Water Heater Loop Hose with Insulation
The first was to insulate the engine cooling water hoses and re-route them to reduce their length. The 7/8 inch ID pipe insulation from Home Depot fits the hoses perfectly. We used some thin mylar and aluminum ducting tape (not the fabric duct tape) to help hold the insulation hose closed. It is best to wrap a piece of tape around the hose every six inches.

The next observation is that the compartment gets warm from the heat expelled through the insulation on the hoses, from the hot water heater, and from the fuel tank when we're running the engines for very long. So we created a small duct to go over the condenser intake and ran the cooling air supply duct to this duct. It is constructed from a piece of 3/8 inch thick foam insulation and is held onto the side of the Sea Frost with velcro. A 4-inch mounting ring connects to the air supply hose.
Sea Frost Cooling Air Duct

  -Terry


Sunday, April 20, 2014

Keeping An Eye On Things: A Boat Monitoring System

It is a good idea to monitor boat systems in order to detect problems before they become major problems. Collecting basic information like engine operating temperatures, refrigeration system temperatures, and battery performance information are a few examples. It is best to gather an information baseline when everything is operating correctly so that abnormal readings are easy to identify. A manual method of recording the information is easy - just record the measurements on paper. Transferring the information to a spreadsheet makes it easy to display as graphs, making it easy to spot trends that may indicate a pending problem.

IR Thermometer Gun
We've been recording engine temperature readings for some time, but only doing it on a sporadic basis and putting the data into a spreadsheet. Even with the sporadic measurements, we've developed a baseline that allows us to determine if there is a problem with one of the engines. (Note: We recommend that everyone capture the data to create a baseline of engine operation. An IR thermometer isn't terribly expensive ($40-$90 on Amazon) and is a great diagnostic tool. Put one on your gift list for your spouse/SO to buy for you.) We have a remote temperature sensing system to show us the refrigeration system temperatures (freezer, fridge, compressor housing). But there is no historical information stored that allows us to determine if (or when) the system is experiencing problems.

My "day job" is computer network design and monitoring, which requires automated systems to collect the large volume of data. Applying those same principles to boat monitoring led me to automate data collection using a single board computer known as a Raspberry Pi. The other attractiveness is that it is a cool project. I'll refer to the Raspberry Pi as "RPi" in the rest of this post. I'm starting with temperature monitoring and will add other features as I go.

I plan to monitor the temperatures listed below. The engine temperature readings are the same as what we've been manually monitoring. We have the Oregon Scientific Clock Weather Forecaster BAR206A and THN132N Wireless Temperature Sensors for monitoring the refrigeration system, but have not recorded measurements. Manually recording refrigeration system temperatures would be useless because of the changes in temperature after the door was opened. Automated temperature recording would let us know how long it takes to return to the desired operating temperature.

Raspberry Pi with Pi Plate Development Board and Acrylic Enclosure
* Ambient air (clipped to the back of the DC panel)
* Freezer plate
* Freezer mid-rack
* Refrigerator mid-rack
* Refrigeration compressor cabinet
* Port and Stbd water heater
* Port and Stbd air conditioners
* Port and Stbd engines
  - Alternator frame
  - Exhaust mixing elbow
  - Raw water inlet
  - Oil pan
  - Cylinder head (one sensor - the ideal would be one next to each injector)

This photo shows the RPi with the attached Pi Plate development board in an acrylic enclosure. The is the fully assembled unit. It measures 6in x 3in x 1.5in. In the foreground is one of the waterproof temperature sensors, which is attached to the white cable that connects to the board. My prototype has three sensors, which I've labeled freezer, fridge, and compressor.
Sample Hourly Temperature Graph

I have a script (a small computer program) that periodically creates graphs of the collected data. All three temperatures are shown on one graph. I'll wait until I get on the boat to refine what types of graphs I want.

The Details


The temperature probe is the DS18B20, which is available in a waterproof version (we'll see, they are probably only water resistant) from sellers on Ebay (search for "waterproof DS18B20"). I found that connecting the DS18B20 using all three wires (Ground, Data, +3.3v) worked the best. I used a "Pi Plate" development board for connections between the RPi and the DS18B20. All sensors can be connected to the same 3-wire bus, which I'll snake around the boat to all the locations. The operating system supports up to 10 temperature sensors. That's not enough for my purposes, so I'll have to generate a new kernel to support many more sensors, probably 30.

The Internet contains many examples of interfacing the DS18B20 temperature sensor with the Raspberry Pi.

I am using the Round Robin Database (RRD) to store the sensor values. RRD is typically used for network management functions. It is very simple and does a good job of storing and displaying time-series data. The current implementation stores a month of samples. I have plenty of storage space and RRD is very efficient, so I'm planning to increase it to several months so that we can see longer term trends.


12V to USB Power Adapter
I needed a way to power the RPi on the boat. The easiest solution was to modify a 12V to USB adapter. This photo shows the adapter with two new wires soldered to it. I wrapped the modified adapter in heat shrink. The red wire connects to an in-line fuse for connecting to the boat's 12V system.

I'll be publishing the scripts that I've developed for this system so that anyone can make their own and can contribute to it.

  -Terry



Monday, April 22, 2013

Leopard 40 Refrigerator Gaskets

We wrote about our experience with the refrigerator and freezer on LUX in It's Freezing In There. Since then, several people have purchased gaskets from coolergaskets.com. Matt (matt (@) coolergaskets.com) is very helpful. John on 2AWESOME reported that the profile 702 gaskets fit exactly, with the same measurements that we made on LUX. The gaskets are without the internal magnets. I don't like the idea of magnets on a boat - they can interfere with compasses. I have a hand-bearing compass that I like to use on the fridge top, which is like a nav station for us on LUX. The magnets are too close to the top for my peace of mind.

Our measurements:
Freezer: 15.0 in wide X 23.25 in high
Fridge:  17.5 in wide X 23.25 in high

Other people have reported slightly larger dimensions. These dimensions should be across the outside of the existing gaskets. Make sure that the measurements match the door facing. There is enough room on the door facing (the fiberglass facing where the gaskets will mate when the door is closed) that the measurements are not critical.

The Coolergaskets are gray, while the ones on LUX are white. But we're happy to change color to get something that seals well. Their price was also reasonable.

I don't know if the other Leopards have similar gaskets. Some Leopards have top-loading fridge/freezer, so the gaskets are probably different. A wider gasket may be desirable in those cases, perhaps the profile 494.

So I think we can say that the quest for Leopard 40 fridge gaskets is over. Tell Matt (the Gasket Guru) that Terry on LUX sent you. Finally, thanks to John on 2AWESOME for checking out the samples I had Matt send him and for being the test case for a set of gaskets.

  -Terry

Saturday, October 27, 2012

It's Freezing In There!


The Saga of the SeaFrost refrigeration system.

When we visited LUX in March 2011 for a week-long cruise around Tortola, we found that the refrigeration system wouldn't stay cold enough to keep our food safe. Unfortunately, we were there on a holiday and the local charter management staff found Alfred, who supposedly knew how to diagnose and repair refrigeration systems. Well, Alfred didn't know a lot. We wound up with a completely broken compressor that wouldn't run. Our temporary solution was to use an ice chest for our food. Upon return to Nanny Cay, another refrigeration person quickly diagnosed a bad compressor, which is what we had diagnosed as well. The new compressor and installation cost about $1400 (ugh!) It then worked correctly.

When we went back in May to bring LUX back to the Chesapeake, the refrigeration system was working, but not as well as we wanted. It was ok for keeping food safe, so we decided to investigate further when we were home.

What was clear is that there was a slow leak. We bought a gas detector and a refrigeration gauge system from Harbor Freight Tools to help us diagnose and repair the source of the leak. We found several suspect connections and were able to tighten them, vacuum the system, and recharge it with 134R refrigerant. The gas detector hasn't indicated any leaks more recently.

The collective wisdom of the Leopard catamaran mailing list on Yahoo was to add refrigerant slowly. The lines should frost all the way through the system. During the discussion, it was funny to hear someone else with a story about Alfred at Nanny Cay, with similar results. If you get any refrigeration system work done on Tortola, be suspect of anyone named Alfred.

After about a month, we found that we needed to add more charge. The loss of refrigerant (i.e. cooling) seemed to correlate with the number of times that the system was fully defrosted. Warming up the entire system to ambient temperature seemed to accelerate the loss of refrigerant. We checked the resistor that determines the run speed of the compressor and there is already a resistor in place that causes it to run at high speed.

An infrared thermometer shows that the exhaust air is 20 degrees warmer than the intake air. We reversed the fan so that air is first drawn over the condenser, then over the compressor. This seems more efficient than the default configuration, though we don't have any actual measurements to back it up.

On one of the recharges, we noticed a small "Pfftt" sound when the low pressure service port cap was removed. The schrader valves are deep in the fittings, so we had to make a trip to the local HVAC supply shop to get a tool to replace them. There is a nice tool that allows replacing the valve without discharging the system, but unfortunately, it didn't fit the Sea Frost system. However, the schrader valve tool that is part of it could be used to tighten the valves. We found that they could be tightened about 1/10 to 1/8 of a turn. So far, so good, but the system hasn't been running long enough for us to know for sure. The freezer is working well, but still runs all the time. We think it should be running half the time.

Door Gaskets

Refrigerator Door, Door Liner, and Taped Refrigerator Opening
We also thought that the door gaskets could be replaced, perhaps providing better seals than the gaskets that are now eight years old. We ordered gaskets that looked like the proper cross-section (number P-2099-8) from Exact-A-Line Gasket, Inc, in Canada. The gaskets arrived and are very nice. We let them sit out for a few days to resume their normal shape after being twisted in the shipping box.

The inner fridge door and gasket are held in place by pan-head screws, which don't seem like the right kind of fasteners to use. It seems to us that flat-head fasteners, countersunk into the door liner would be better. Surprisingly, the door itself isn't fully insulated. The insulation is concentrated in the inner liner. We used plastic taped over the door to keep the cold air in the refrigerator while the door surgery was under way. All three are shown here.

The new gasket fit the refrigerator door extremely well. Unfortunately, when we reassembled the door, we found that it didn't compress as much as the old gasket and that we could only shut the door by sitting on the floor and pressing the door closed with a foot. The door wouldn't stay latched. And in addition, about 1/8 of the gasket was not making contact with the door facing, which is really not good.

Off came the new gasket and back went the old gasket, after it was thoroughly cleaned and inspected. The old gasket is still in good condition. It is flexible and seems to seal all around. The replacement was to eliminate the seal as a source of air leakage, more on the freezer compartment than the freezer compartment. As a result of the work, we replaced the screws with counter-sunk flat-head screws, which should help the lay of the gasket on the door.

There are other gaskets available from Exact-A-Gasket and we'll be contacting them to discuss options and see which one works best for us.

Update 2/22/2013

We have since found coolergaskets.com, and their profile 702 looks like an exact replacement for the existing Leopard 40 refrigerator/freezer door gaskets. Another option is their profile 494, which is about 1/16-inch shorter in height and has a 5/8-inch wide face. The wider face would have a lower pressure (lb per sq in), but may seal better due to the larger mating surface. Both of these gaskets are gray, not white. One of the cruisers is going to try this gasket to see how well it works. We won't be able to try new gaskets until June 2013, when we bring LUX back from the Bahamas to the Chesapeake. 

Our door measurements are:
Freezer: 15.0 in wide X 23.25 in high
Fridge:  17.5 in wide X 23.5 in high
George on Matador said that he measured the Freezer as 15.25 wide, and the other measurements the same as ours. John on 2AWESOME was able to get our Exact-a-line gasket for the freezer to work, but had the same problem that we had on the fridge door. So the 15.0 in measurement worked for John's freezer (we had not tried the freezer gasket after the fridge door didn't work).

Additional Update on 8/2/2017

We found that the refrigeration system would gradually lose effectiveness after a period of not running it. After some discussion, we decided that there was a leak in the low pressure side. When we turned the system off, the higher pressure in the low pressure side would leak refrigerant. So we called Nate Horton (Horton Marine Services in Annapolis, MD) to take a look. He quickly found a leak at the brazed connection of the low pressure (blue) maintenance connector by pressurizing the system with nitrogen. It was a quick fix and it worked well for a couple of years. This spring (early 2017), we noticed that it wasn't working as well as it had in the past. It sat all winter without running, so maybe there's still a slow leak somewhere. We had some left over refrigerant in a container with a fill hose, so we added it - about 1/3 of the can. That restored the operation and the plates get frosted again like they used to.

We have also lined the refrigerator and freezer with double sided TechFoil. It's like bubble wrap with aluminum foil on both sides. Inexpensive insulation and it doesn't consume much space. We lift it to allow it to dry underneath when we defrost the freezer.

We also added the digital control, which seems to have made a big difference in how well the freezer performs. It runs a bit over 50% of the time.

Update 11/06/2019

We decided to add a second gasket to the door seals to effectively create a dual seal against air leakage. How do we make sure that the second gasket it working? Our GoPro camera was linked to our iPad, placed inside the refrigerator with a light, and positioned to watch the seal as the door was closed. The main gaskets fit against the face of the refrigerator cabinet. But the door is recessed and the inside edge is the perfect place for a second gasket. A small profile gasket from Home Depot did the trick.


Last fall, we finally decided to replace the refrigeration compressor unit. The expansion valve had originally been mounted in the area where the electrical distribution panel is located, under the freezer/refrigerator. Condensation would form on it and drip into the bilge, creating a humidity problem. We talked with Cliff Wasser, who does local refrigeration work in Annapolis, MD. He recommended a change from R134A to R410 refrigerant and a new compressor unit. He agreed with the idea of moving the expansion valve into the top of the freezer cabinet. It has worked flawlessly since then. We're able to keep ice cream in the freezer compartment and not freeze food that's in the refrigeration compartment as long as we close the baffles between them. The compressor also doesn't run as much or generate as much heat as the old R134A compressor.

The air in the area under the bunk gets quite warm from the hot water heater and from the fuel tank when we motor for any length of time. We decided that input to the condenser/compressor should be coming from the cabin, not from the hot compartment air. A box was constructed from 3/8-inch pink hard foam board and a hose connects it to the cabin air supply. The box is held onto the Seafrost with velcro strips. The fan is oriented so that incoming air goes through the condenser before going over the compressor.

  -Terry